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enforce pit management, and carefully monitor for any discrepancies during
                          253
                   trips.”

                          Joseph Keith, a Sperry‐Sun mudlogger, testified that the rig crew was
                   “moving a lot of mud around from different pits, reserve pits, active pits, trip
                                                                                        254
                   tanks [and] sand traps.  They were moving a lot of mud around.”   Keith
                   testified that he was concerned about this because he “couldn’t really monitor
                   the volumes in the pits correctly.”   Keith also testified that the activities
                                                       255
                   occurring onboard the Deepwater Horizon were not consistent with Transocean’s
                   kick prevention procedures.   Nevertheless, at no point prior to the blowout,
                                                 256
                   did Keith issue a stop‐work order because, according to his testimony, he “just
                   didn’t think of it at the time.”   Keith testified, however, that the high level of
                                                  257
                   mud‐moving activities should have resulted in a stop‐work order from someone
                   on the rig.
                              258

                          Dr. Smith analyzed available data and, in his report, detailed what Keith
                   and the rest of the crew would have observed had they properly monitored the
                   well.  Just after 8:00 p.m., an increase of main pit volume by 500 barrels, likely the
                   result of the transfer of seawater into the main pit, precluded the crew from
                   using pit gain as a monitoring tool.  According to Dr. Smith, not having this tool
                   available complicated kick detection efforts and was not consistent with proper
                   pit management and monitoring.
                                                      259

                          Dr. Smith concluded that the crew could not properly monitor the well
                   and detect kicks from 8:38 p.m. to 8:56 p.m. on April 20.  During this time, the
                   flow‐out was significantly less than the flow‐in, in a situation where lost returns
                   were unlikely.  At the same time, the trip tank volume was increasing rapidly,
                   and the data showed that there was some volume increase in the main pits.
                   Given the complications created by conducting multiple operations
                   simultaneously, it is unlikely that the crew was able to evaluate these signals that
                                           260
                   a kick was in progress.



                   253  TRN‐USCG‐MMS00043810.
                   254  Keith testimony at 39.
                   255  Id. at 98.
                   256  Id at. 39.
                   257  Id. at 81.
                   258  Id. at 82.
                   259  Smith Report at 22.
                   260  Id.


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