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approximately 9:20 p.m., Jason Anderson, the toolpusher, told Miles Ezell, the
                                                                                                266
                   senior toolpusher, that the displacement was “going fine….I’ve got this.”   Ezell
                   testified that Anderson “had more experience as far as shutting in for kicks than
                   any individual on the Deepwater Horizon.”   The Panel found evidence that a
                                                               267
                   significant volume of hydrocarbons had already entered the wellbore, but the
                   Panel found no evidence that the Transocean rig crew had any awareness that
                   the well was flowing or experiencing a kick at this time.

                              C.     Rig Floor Response


                          At approximately 9:30 p.m., Revette identified a pressure difference
                   between the drill pipe and the kill line and shut down the pumps to investigate.
                   The Sperry‐Sun data indicated that the drill pipe pressure initially decreased
                   when the pumps shut down.  However, the drill pipe pressure then increased by
                   approximately 550 psi during the next five minutes while the kill line pressure
                   remained lower.  One crew member testified that the driller and the toolpusher
                                                                   268
                   had concerns about this pressure differential.

                          The rig crew then attempted to bleed off the drill pipe (i.e., open the well)
                   to eliminate the pressure differential, which briefly caused the drill pipe pressure
                                269
                   to decrease.   Given that the rig crew at this time decided to bleed off the drill
                   pipe pressure, they likely still did not understand that the well had begun to
                   flow.  Bleeding off drill pipe pressure during a kick is not an industry‐accepted
                   practice.

                          At 9:38 p.m., the drill pipe pressure began to build back up.  Dr. Smith
                   concluded that, at this time, the rig crew routed flow to the trip tank to check
                                                   270
                   whether the well was flowing.   At approximately 9:42 p.m., the crew detected
                   flow and diverted the gas to the mud gas separator.  At the same moment, or
                   shortly thereafter, the rig crew activated the upper annular preventer, after the
                   mud from the well was already flowing on the rig floor.  The Sperry‐Sun data
                   indicates the annular preventer was activated at 9:43 p.m., and by 9:47 p.m., the
                   variable bore ram had been activated.  By this time, the rig crew knew that a well
                   control event was occurring.  The Transocean well control manual provides that
                   the crew should activate the BOP’s blind shear ram (“BSR”) as the last step in

                   266  Ezell testimony at 282.
                   267  Id. at 311.
                   268  Testimony of David Young, Joint Investigation Hearing, May 27, 2010, at 258‐59.
                   269  Robinson testimony at 284‐85.
                   270  Smith Report at 14.


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