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to the mud gas separator.  Transocean’s well control manual did not clearly state
                   to go to the diverter if the flow event is unknown.  The ambiguity within the
                   Transocean well control manual on when to use the diverter and not the mud
                   gas separator was a contributing cause of the response failure.

                          At approximately 9:48 p.m., several of the gas alarms sounded.  Within
                   minutes, approximately 20 gas alarms were sounding, the result of extremely
                   high levels of gas concentration.  Yancy Keplinger, the senior dynamic
                   positioning officer, went to the video monitor and saw large amounts of mud
                   being ejected.  Shortly afterwards, Andrea Fleytas, the dynamic positioning
                   officer, got a call from the rig floor, which informed her that there was a “well
                   control problem.”  Fleytas told the Panel she received a phone call from the
                   engine room, but she never told the engine room personnel to perform an
                   emergency shutdown.  The initial explosion occurred approximately 30 seconds
                   to a minute after the first gas alarm.  At approximately 10:00 p.m., the general
                   alarm and fire alarm on the Deepwater Horizon sounded and the rig began to list
                   to one side.  Only then did Keplinger make an announcement to muster and
                   prepare to evacuate.  Personnel were not told to evacuate until approximately
                   twelve minutes after the first gas alarm went off.  The failure of the personnel
                   on the Deepwater Horizon bridge monitoring the gas alarms to notify the
                   Deepwater Horizon crew in the engine control room about the alarms so that
                   they could take actions to shut down the engines was a contributing cause of
                   the response failure.

                              E.     Response Failure Possible Contributing Causes

                          The crew was unaware of the volume of the hydrocarbon influx associated
                   with the blowout.  The rig floor crew’s inability to determine the location of
                   the kick in relation to the BOP stack and the volume of hydrocarbons coming
                   to the rig in a matter of seconds was a possible contributing cause of the
                   response failure.

                          The Panel found no evidence that Jason Anderson, Transocean driller,
                   who was identified in the Transocean procedures as the individual who should
                   initiate the emergency disconnect system, attempted to do so once the
                   hydrocarbons were past the stack.  There is evidence that the rig crew activated
                   the upper annular and upper variable bore ram when the hydrocarbons were
                   past the stack.  There is also evidence that Chris Pleasant, Transocean subsea
                   engineer, attempted to activate the emergency disconnect system some time after
                   the explosions had disabled communications with the BOP stack.  The rig crew’s



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