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C.     Kick Detection Failure Possible Contributing Causes


                          On March 8, 2010, the Deepwater Horizon crew experienced a well control
                   event that went undetected for 30 minutes.  Ten of the eleven individuals on
                   duty on March 8 during the undetected kick and well control event were also on
                   duty during the April 20 blowout.  According to John Guide, Transocean rig
                   management personnel admitted to him that those individuals involved with the
                   March 8 incident had “screwed up by not catching” the kick.  Although BP has
                   internal requirements to conduct investigations into all drilling incidents, BP did

                   not do so for the March 8incident.  BP’s failure to perform an incident
                   investigation into the March 8, 2010 well control event and delayed kick
                   detection was a possible contributing cause to the April 20, 2010 kick detection
                   failure.

                          The Panel found no evidence that, during cement pumping, BP shared
                   information with either the Deepwater Horizon rig personnel or Transocean shore‐
                   based employees about the increased risks associated with the Macondo
                   production casing cement operations, such as, the decision not to include a
                   second cement barrier above the wiper plug and the anomalies encountered
                   during cement pumping.  BP’s failure to inform the parties operating on its
                   behalf of all known risks associated with the Macondo well production casing
                   cement job was a possible contributing cause of the kick detection failure.

                          BP decided to combine two lost circulation material pills, and use this
                   combined material as a spacer in the Macondo well.  The presence of this spacer
                   allowed viscous material to be across the choke and kill lines during the negative
                   test and possibly plugged the kill line.  If the kill line was plugged, it could have
                   led to the pressure differential between the drill pipe and kill line.  BP’s use of
                   the lost circulation material pills as a spacer in the Macondo well likely
                   affected the crew’s ability to conduct an accurate negative test on the kill line
                   and was a possible contributing cause of the kick detection failure.

                          John Guide, the BP well team leader, believed that the Deepwater Horizon
                   crew had become “too comfortable” because of its good track record for drilling
                   difficult wells.  Ross Skidmore, a BP contractor on the rig on April20, testified

                   that the crew became complacent after completing drilling because “when you
                   get to that point, everybody goes to the mindset that weʹre through, this job is
                   done.”  The complacency on the Deepwater Horizon could be attributable to the
                   crew not having access to all of the well data (OptiCem reports) available to BP
                   personnel onshore and the well site leaders on the rig.  The overall complacency



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