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at about 5:52 p.m. and attempted to bleed‐off the drill pipe pressure.  After three
                   unsuccessful attempts, the crew eventually justified the pressure as a “bladder
                   effect.”  The rig crew did not realize the well was flowing until mud was
                   discharging onto the rig floor.  The Deepwater Horizon crew’s hesitance to shut‐
                   in the BOP immediately was a possible contributing cause of the kick
                   detection failure.

                          The MMS‐approved APM called for two negative tests.  This would allow
                   for the greater opportunity to detect hydrocarbon influx in a staged test since the
                   first test would have been to the wellhead and the second test would have been
                   to the depth of 8,367 feet.  BP’s failure to conduct the first of the two negative
                   tests was a possible contributing cause of the kick detection failure.

                          When the Deepwater Horizon crew resumed pumping the returns
                   overboard at 9:15 p.m., the flow bypassed the Sperry‐Sun meter due to its
                   downstream location off the flow return trough.  Consequently flow‐out data
                   could not be adequately monitored by personnel, such as the Sperry‐Sun
                   mudloggers, who were responsible for monitoring these data.  The rig crew’s
                   decision to bypass the Sperry‐Sun flow meter while pumping the spacer
                   overboard was a possible contributing cause of the kick detection failure.

                          Well control training historically has not addressed situations, such as
                   conducting a negative test in that one is “inviting” a well control event to occur.
                   Additionally, displacement operations that put the well in an underbalanced
                   condition should be closely monitored throughout displacement operations.  The
                   failure of BP’s and Transocean’s well control training and MMS requirements
                   to address situations, such as negative tests and displacement operations, was
                   a possible contributing cause of the well control failure.

                              D.     Response Failure Contributing Causes

                          The rig crew’s decision to use the mud gas separator instead of the
                   diverter accelerated the likelihood that the gas on the rig would ignite.  The
                   decision to use the mud gas separator during the well control event was a
                   contributing cause of the response failure.

                          Once members of the drill crew identified the increase in drill pipe
                   pressure, they checked the well for flow.  At approximately 9:42 p.m., the crew
                   detected flow and diverted the gas to the mud gas separator.  The rig crew was
                   not able to determine the magnitude of the flow when it made the decision to go



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