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                   noon on April 20.  The pressures in the well remained constant during testing.
                   Dr. Smith, an expert retained by the JIT to review test data and other
                                                                                    224
                   information, found the positive pressure test to be acceptable.

                                   3.    Negative Tests Conducted on April 20


                          Without much time to consider changes in the temporary abandonment
                   procedures, on April 20 the Deepwater Horizon crew began work toward
                   conducting the critical negative test to evaluate well integrity.  Before starting the
                   test, the crew displaced mud from the wellbore with seawater, which would
                   simulate well conditions after the well had been temporarily abandoned.

                          The first step of the negative test was to displace the riser boost line, the
                   choke line, and the kill line with seawater.   These efforts began at
                                                                225
                   approximately 4:00 p.m. on April 20.  Over the next 30 minutes, the crew
                   pumped the 454 bbls of spacer (consisting, as discussed above, of mixed lost
                   circulation materials).  Around 4:30 p.m., the crew then pumped approximately
                   352 barrels of seawater into the wellbore, which took approximately 25 minutes.
                   After pumping the spacer and seawater, seawater should have been located
                   down the workstring and in the wellbore from 8,367 feet to 5,117 feet total depth
                   and the spacer should have been located just above the seawater ‐ from 5,117 feet
                                226
                   to 3,707 feet.

                          After the displacement, the rig crew should have seen a drill pipe pressure
                   of 1,610 psi, based on hydrostatic fluid calculations.  However, the electronic data
                   indicates that the drill pipe pressure was 2,339 psi.  This reading was more than
                   700 psi higher than it should have been.  If the crew saw this information, they
                   should have taken measure to resolve this anomaly because it may have
                   indicated that the spacer remained below the BOP stack (and could have clogged
                   the choke or kill lines).  227   This problem could have been resolved by continuing
                   the displacement (through the choke line) to ensure that all mud and spacer had
                   been removed from the wellbore below the BOP stack.  This method of “cleaning
                   up the well” would not have compromised the function of the spacer because
                                                                                       228
                   most of the spacer was already in the riser above the BOP stack.

                   223  Smith Report at 7; Deepwater Horizon IADC Daily Drilling Report, April 20, 2010.
                   224  Smith Report at 8.
                   225  This first step was different from the first step in the MMS‐approved APM.
                   226  Id. at 9.
                   227  Id.
                   228  Id. at 18‐19.


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