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that Sims and O’Bryan met with Kaluza at some point to discuss the positive
                                                                                               233
                   pressure test and how the crew would be lining up for the negative test.   But
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                   the crew did not consult O’Bryan or Sims about the actual negative test results.

                          Around 5:30 p.m., after the first unsuccessful negative test, the rig crew
                   began to set up for another negative test, which began by bleeding off the drill
                   pipe and closing an internal valve in the drill pipe for 20 minutes.  Once this
                   valve was closed, the crew was no longer capable of monitoring the drill pipe
                   pressure.

                          Around 6:00 p.m., the crew bled the pressure from the drill pipe to the
                   cementing unit.  At that time, the drill pipe was shut in at the cementing unit,
                   and the pressure on the drill pipe increased to 1,400 psi after 30 minutes.  As the
                   pressure on the drill pipe increased, the kill line pressure also steadily increased
                   but only to 140 psi.  This pressure differential between the drill pipe and the kill
                   line was another indicator that the negative test was not successful.

                          Around 6:45 p.m., the crew pumped a small amount of fluid into the kill
                   line to make sure it was full for another negative test.  At approximately 7:15
                   p.m., the crew opened the kill line to monitor for pressure/flow consistent with
                   the APM approved by MMS.  After approximately 40 minutes of no flow or
                   pressure observed on the kill line, the crew and the BP well site leaders deemed
                   the negative test successful and began operations to complete the displacement
                   of drilling mud with seawater.  Notwithstanding multiple anomalies that the
                   crew encountered during the several failed negative test attempts, the drill crew
                   and the BP well site leaders decided not to flush the system and conduct a new
                   negative test.

                          Testimony from rig personnel involved with the negative test reflects that
                   they believed that they had successfully tested the integrity of the well by
                   checking for flow on the kill line.  Kaluza stated that “[i]t was not
                   flowing…Absolutely no flow.”   Miles Ezell, Transocean senior toolpusher,
                                                    235
                   testified that Jason Anderson told him that “[i]t went good . . . We bled it off.  We



                   rate of “days away from work.”  They also planned to discuss the rig’s financial performance
                   (costs compared to AFEs) and ongoing risk and hazard recognition.  See BP‐HZN‐MBI129014.
                   233  Testimony of Patrick O’Bryan, Joint Investigation Hearing, August 26, 2010, at 360, 374; Sims
                   testimony, May 29 2010, at 178.
                   234  O’Bryan testimony at 443; Sims testimony, May 29, 2010, at 179.
                   235  BP‐HZN‐MBI00021264.


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