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DNV stated that its tests of the blue pod in its as‐received condition
                   demonstrated that “the 27 Volt battery in the Blue Pod had insufficient charge to
                   activate the solenoid 103B.”  DNV noted that there were no records showing that
                   the batteries in the AMF system were tested during a factory acceptance test in
                              353
                   June 2009.   DNV further noted that tests for the 27‐volt battery conducted in
                   July 2010 (when the BOP was retrieved) “reported the battery level to be out of
                                  354
                   specification.”

                          The Deepwater Horizon crew did not have the ability to monitor the subsea
                   electronic module (“SEM”) battery power supply, although the Panel is aware of
                   technology that exists that would allow Transocean to perform this monitoring.
                   If the crew had been able to monitor the SEM power supply, they could have
                   known the real time condition of the AMF batteries.

                          Two other theories regarding the failure of the BOP stack were advanced
                   during JIT hearings.  The first is that the hydraulic systems that powered the BSR
                   did not have enough power to cause the blind shear rams to fully close and seal.
                   A Cameron representative stated:

                          There is a possibility that the shear ram could have been functioned not
                          through the high pressure circuit but through the manifold pressure,
                          which would be 1,500 PSI, and itʹs possible that if that happened, we
                          wouldnʹt have near enough hydraulic force pressure ‐ you could not
                          generate enough force with that pressure to cut the pipe.  In fact, itʹs very
                          likely that the pipe would only be dented and not shear all the way
                          through, exposing the ram to the flows that we all have heard about.  Itʹs
                          also possible that for whatever reason the hydraulic system wasnʹt up to
                          the game that day and didnʹt have sufficient pressure to close it.  It is
                          possible that the solenoid valve, which when tested by DNV in Michoud,
                          operated intermittently, sometimes it wouldnʹt operate at all and other
                          times it would operate for a handful of seconds.  And it is possible that if
                          the deadman fired and the solenoid valve did exactly what it did at
                          Michoud, that the ram could have partially deployed and not gone all the
                          way across.
                                       355





                   353  Id.
                   354  Id. at 170.
                   355  McWhorter testimony at 144‐45.


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