Page 68 - test2
P. 68

hanger and seal assembly remained properly seated in the 18‐3/4 inch high
                                                                                                    154
                   pressure housing, where it had been placed on April 19 prior to the blowout.

                          Additional evidence from the intervention operations also tends to
                   eliminate this first well flow scenario.  On September 10, during the well
                   intervention operation, BP conducted a positive pressure test of the 9‐7/8 inch
                   production casing in the Macondo well by pumping 6 bbls of 13.2 ppg drilling
                   mud down the BOP kill line and reached an instantaneous shut‐in casing
                   pressure (ISICP) of 4,270 psi.  The kill line was then shut in and, after 30 minutes,
                   the shut‐in pressure remained at 4,158 psi, therefore revealing no flow through
                   the annulus.

                          On September 11, following installation of the lock‐down sleeve, BP
                   successfully pressure tested the lock‐down sleeve seal to 5,200 psi, which
                   indicated that the well hanger was properly seated because otherwise, annular
                                                        155
                   flow would have lifted the hanger.

                          On September 22, Schlumberger used an isolation scanner tool to log the
                   characteristics of fluid in the annulus between the mud line and 9,318 feet
                                     156
                   measured depth.   This log evaluated, among other things, whether the fluid in
                   the annulus included “free gas.”  Based on the logging data, Schlumberger
                   determined that free gas was not present in the annulus below the BOP.  The
                   absence of free gas in the annulus provides strong evidence that hydrocarbons
                   were not present in the annulus during the blowout.

                          On October 7, the intervention team perforated the 9‐7/8 inch production
                                                                                                157
                   casing between 9,176 feet and 9,186 feet to monitor pressure and returns.   The
                   drilling mud in the interior of the casing at the time was approximately 14.3 ppg
                   synthetic‐based mud (“SBM”).  Hydrocarbons, if present in the annulus, would
                   have exhibited a much lower density.  When fluids of different densities meet at
                   an opening, gravity and the “u‐tube” effect typically cause the more dense fluid


                   154  DDII IADC Report, 9/11/10 (TRN‐USCG_MMS‐00043342).
                   155  DDII IADC Report, 9/11/10 (TRN‐USCG_MMS‐00043342).  A “well hanger” is a long string of
                   production casing that hangs from a casing hanger inside the wellhead.
                   156  DDII IADC Report 9/22/10 ‐ TRN‐USCG_MMS‐00043388.  An isolation scanner tool is used to
                   evaluate a cement job by taking measurements to help distinguish solids from liquids in the
                   wellbore.  The tool can identify potential channeling and can evaluate whether a cement job has
                   achieved zonal isolation.
                   157  DDII IADC Report 10/7/10 (TRN‐USCG_MMS‐00043449).  This was done using a perforating
                   gun and well testing equipment.


                                                             63
   63   64   65   66   67   68   69   70   71   72   73